Suresh Kumar, M and Madan, M and Venkataswamy, MA and Sujata, M and Parameswara, MA and Bhaumik, SK (2005) Analysis of failed Tail Gear Box housing of a helicopter. Project Report. National Aerospace Laboratories, Bangalore.
Full text not available from this repository. (Request a copy)Abstract
A failed Tail Gear Box (TGB) housing of a helicopter was analyzed. Analysis showed that the gearbox failed by fatigue. Fatigue cracks initiated at the mounting lugs and propagated by low cycle fatigue. There were no metallurgical and/or mechanical abnormalities associated with fatigue crack initiation. Fatigue appears to be stress related. The possibility of excessive load/vibration on the TGB housings in question may be examined.
| Item Type: | Proj.Doc/Technical Report (Project Report) |
|---|---|
| Uncontrolled Keywords: | Helicopter;TGB housing;fatigue |
| Subjects: | AERONAUTICS > Aeronautics (General) CHEMISTRY AND MATERIALS > Chemistry and Materials (General) |
| Division/Department: | Materials Science Division, Materials Science Division, Materials Science Division, Materials Science Division, Materials Science Division, Materials Science Division |
| Depositing User: | Mrs Manoranjitha M D |
| Date Deposited: | 14 Nov 2011 10:12 |
| Last Modified: | 14 Nov 2011 10:12 |
| URI: | http://nal-ir.nal.res.in/id/eprint/9993 |
Actions (login required)
| View Item |

